Brian's hypothesis about fin blinding is absolutely sound and may very well have been a significant contributing factor to this unfortunate flight.
However, the flight made with the rocket a year earlier on the M2100G gives us some clues as well.
That flight was still fairly "wiggly" for the first second or so, and that green motor burns a lot faster than the Dark Matter motors. The M1075DM has less than half the initial thrust of the M2100G. If it was slightly unstable with the bigger punch of the M2100G, the M1075DM was always going to have trouble getting this rocket to a safe speed very quickly.
The rails in both flights look incredibly short (6' rails maybe?). The Mongoose 98 is only an 8' tall bird (unless he modified it). Assuming the top rail button was somewhere around the middle of the rocket, that means he only had positive control of the rocket on the rail for about 2'-3'. That feels crazy short.
Finally, the nosecone displacement on the M1075DM flight seems to be significant. It is clear in the M2100G flight video that the nosecone was firmly seated in the airframe, so it is difficult to believe it was supposed to fly with the nosecone sticking out that much. I can't imagine why that wouldn't be noticeable on the pad, but it feels like the nosecone issue is another contributor to this flight's outcome.
Combine a motor with a relatively weak initial thrust, a very short rail, possible fin blinding from the camera shroud, a rocket that is already marginally stable by design and a displaced nosecone, it is not surprising it went sideways. The more important discussion is that all of those factors are extremely avoidable. This was not an "experimental" flight (and, to be clear, I am highly supportive of experimental flights conducted under safe conditions - pushing boundaries furthers the hobby/science) - this was a "normal" flight that, seemingly, did not take into account a number of obvious issues.