rocketfarmer
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- Joined
- Nov 20, 2009
- Messages
- 12
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I will post up some photos soon... Well, Lets start with the rebuilt Breaking Bad. I prepared a 4 grain Aerotech 38mm for the maiden rebuilt flight. The rocket ripped off the pad and then at 100-150 ft she blew apart, the FC landing on the forward end smashing the body tube again. the Electronic bay, payload section, and nose came down onto the LSO trailer smashing the Elec Bay and both of the aft aluminum Blast containers narrowly missing the who ever was announcing at the time. will I rebuild it again??? probably because I cant stand to be beat by this!!! Tore the motor apart and it was assembled 100% correct so I have no reason yet as why it blew out forward ruining the rocket and melting down the Awesome color matched Binder Design Chute built specifically for the Breaking Bad rebuild. So... I was also preparing the Brand New never flown LOC BRUISER EXP3 with a Large Cesaroni K Vmax to rip it into the sky but got cold feet after the Breaking Bad fiasco. I decided to first launch it with a large I Vmax with just the Fincan and Nose cone more like a basic bruiser with single deploy. I prepared the motor and headed to the RSO table where I realized I had prepared the delay as if running the K motor, so out came the motor I ran the near mile back to my pit tables and plopped the I motor down next to where I was previously building the K. I removed the forward end and drilled the delay out from 13 to 7 seconds. now back to the line and to the rail she went...... It lit and then......HOLY SLOW..... In my head I said That is not a Vmax as I heard the same words over the PA. 50-60 feet in 1-2-3 seconds of burn..... AHHH WTF........... now the 7 sec delay seams reallllllllyyyyy long itsef... LOL I had just enough time for the previous thoughts before the rocket hit the ground completely sideways. Not bad damage for a big rocket with no chute. I will trim less than 6 inches from the Fincan bodytube and be back sunday. I was in a hurry to leave as I was already late for another commitment so I didn't even look at the thing till this morning. I opened the Tinted topper hatch and there it was.... THE ANSWER..... in my rush back from the RSO to drill the delay I mistakenly picked up the K motors nozzle and installed it on the I motor.. Too much nozzle means too little thrust.... I screwed myself by rushing again!!!! I hate me today:cry: Lesson Learndededed..... SLOW DOWN..... DONT RUSH..... if I don't have the time I wont make the flight..