Tonimus
Well-Known Member
- Joined
- Jul 8, 2014
- Messages
- 1,511
- Reaction score
- 11
For those who have seen my other threads, The Neutral Zone is currently our largest rocket and was designed with being flown on seven motors. This weekend, that happened. The rocket is about 11.5' tall, weighs 50# loaded for flight.
Transport out to the pad is easier in pieces:
On the trailer pad waiting for igniters:
Igniters being installed:
Sitting on the pad at 500':
Igniter lights:
And the flight video:
[video=youtube;z103_N7FGso]https://www.youtube.com/watch?v=z103_N7FGso[/video]
After action: All motors lit. Slight wiggle in rocket was likely due to motors coming to pressure at different times. Main tangled on deployment, but landed safely under drogue. Main was packed in a d-bag and shock cord was z-folded and taped for management. I do not know why it tangled. Next may be a non-tethered d-bag.
Overall, the flight went VERY well and the airstart electronics performed wonderfully. The rocket went just over 2300 feet and got quite a reaction from the crowd. We here are very happy with the progress we've made with the design.
A couple "Thank You"s for those who helped one way or another in this project:
Upscale CNC (wingarcher) for cutting fins and rings
OneBadHawk (onebadhawk) for very custom recovery gear
Eggtimer Rocketry (cerving) for flight computers and airstart programming help
Connor (conman) for assembly of the above
James, (smapdiage9) for coming through with two wifi switches after I cooked one of mine
BuyRocketMotors.com (pyrobob) for suggesting some motors that should be easier to light
And anyone else who helped out, THANK YOU ALL!
Transport out to the pad is easier in pieces:
On the trailer pad waiting for igniters:
Igniters being installed:
Sitting on the pad at 500':
Igniter lights:
And the flight video:
[video=youtube;z103_N7FGso]https://www.youtube.com/watch?v=z103_N7FGso[/video]
After action: All motors lit. Slight wiggle in rocket was likely due to motors coming to pressure at different times. Main tangled on deployment, but landed safely under drogue. Main was packed in a d-bag and shock cord was z-folded and taped for management. I do not know why it tangled. Next may be a non-tethered d-bag.
Overall, the flight went VERY well and the airstart electronics performed wonderfully. The rocket went just over 2300 feet and got quite a reaction from the crowd. We here are very happy with the progress we've made with the design.
A couple "Thank You"s for those who helped one way or another in this project:
Upscale CNC (wingarcher) for cutting fins and rings
OneBadHawk (onebadhawk) for very custom recovery gear
Eggtimer Rocketry (cerving) for flight computers and airstart programming help
Connor (conman) for assembly of the above
James, (smapdiage9) for coming through with two wifi switches after I cooked one of mine
BuyRocketMotors.com (pyrobob) for suggesting some motors that should be easier to light
And anyone else who helped out, THANK YOU ALL!