- Joined
- Sep 16, 2010
- Messages
- 77
- Reaction score
- 7
R.I.P. Mega Der RedMax 6/20/14
Today was a beautiful morning to fly my Mega RM! First flight was on a AT G76-4 Green motor. Beautiful flight to 800ft, according to Altimeter 2. The second flight was on a G64-7 White Lightning drilled out to a 4 second delay. Little did I know that this would be its last.
The motor ignited and the rocket lifted off the pad about two inches and then BOOM!. The nose cone ejected on the pad and the motor casing (what was left of it) shot out the bottom with a shotgun blast. Thankfully both grains self extinguished The force was so great my AT Mantis pad broke one of its plastic leg mounts and the entire pad fell over.
I attached some pictures to see if the TRF hive collective can help me analyze what went wrong. I gathered up the debris to do a post mortem. The case failed immediately below the forward closure. The failure is so perfect, you would think it was cut off with a hack saw. I suspect black powder leakage but I am not sure. The red cap is still on and most of the BP seems to be there. The outside of RM is intact but the motor mount tube is totally shot, only about 3 inches of it left.
I have filed a MESS report already. The case is less than a year old so AT should warranty it and the reload. What about the rocket and the pad? Do I add them to the spare parts pile?
Thanks
Jim
Today was a beautiful morning to fly my Mega RM! First flight was on a AT G76-4 Green motor. Beautiful flight to 800ft, according to Altimeter 2. The second flight was on a G64-7 White Lightning drilled out to a 4 second delay. Little did I know that this would be its last.
The motor ignited and the rocket lifted off the pad about two inches and then BOOM!. The nose cone ejected on the pad and the motor casing (what was left of it) shot out the bottom with a shotgun blast. Thankfully both grains self extinguished The force was so great my AT Mantis pad broke one of its plastic leg mounts and the entire pad fell over.
I attached some pictures to see if the TRF hive collective can help me analyze what went wrong. I gathered up the debris to do a post mortem. The case failed immediately below the forward closure. The failure is so perfect, you would think it was cut off with a hack saw. I suspect black powder leakage but I am not sure. The red cap is still on and most of the BP seems to be there. The outside of RM is intact but the motor mount tube is totally shot, only about 3 inches of it left.
I have filed a MESS report already. The case is less than a year old so AT should warranty it and the reload. What about the rocket and the pad? Do I add them to the spare parts pile?
Thanks
Jim
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